Hello all,
I am building an onStep system to motorize my old GP mount.
I have chosen to use a Wemos D1 R32 + CNC3 to make it simple.
The first tests after having uploaded the firmware are done with LX200_onstep INDI driver.
To do it I use the Wemos D1 R32 alone. All connect fine but the INDI driver crashed after the first goto simulation.
Before going further in exploration of the problem I have a question for the one that use onstep: have you find similar problems ?
Thanks